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Morrie's 912 Journal
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12/22/03: A retest of the compression on #1 today revealed that the exhaust valve we lapped has seated and now the compression is sitting at 150 lbs. All 4 cylinders are now between 145 and 150 lbs. The engine still has a smal oil leak from the 1-2 cylinder side, but it does not appear too serious. I also replaced the braided lines which go to the bypass filter, as they were old and seeping. While I had them off, I removed the bypass can from the car and soaked it in chem dip to clean it and discovered that there is a small port drilled into the center tube of the bypass filter. I wowuld imagine this is part of the functionality of the filter, and mine was plugged. I'd suggest clearing this port with a paper clip on your next oil change. these filters do limited good as it is, why push our luck! My carb butterflies look like a solar eclipse when they ar closed. the lack of sealing is making it impossible for me to set a low idle speed. The carbs are going to be overhauled by John Benton then we should be all set!
11/22/03: This is the big day. I have been commenting throughout the journal that the engine has compression issues.
Cylinder #1 has 120 lbs, which is tolerable by my standards but on the weak side. It has remained stable at 120 lbs since I
first tested the compression. A Leakdown test indicated an exhaust valve that needed help, air escaping from the tailpipe
was the tell tale sign. #2 delivers numbers in the 140 to 145 lb range, not a problem. #4 is like 2, so no concern there
either. The serious issue lies with cylinder #3, where the compression began at a meager 100 lbs at first test and has since
worked its way down to 90. I have no reason to believe it will do anything but get worse, so this, coupled with numerous oil
leaks, has prompted me to do some engine work.
I have no intention of making this a full teardown and rebuild. I have no budget for such a venture. I purchased a set of
rings, pushrod tubes, and a top end gasket set in the hopes that #1 is just a cruddy valve and #3 possibly a seal of some
kind. The results of this effort proves that it really was necessary to give the motor a hand.
"Turkey Rebuild." That's what Harry Pellows refers to an engine like mine, at least the one we started with. We did clean
up the #1 exhaust valve, with disappointing results. We lapped the seat and cleaned the valve, and still 120 lbs of
compression. The big find was just how poorly assembled the top end was. Here are just a few of the things we found:
o Rod nuts holding exhaust pipes to studs
o Head washers either missing or doubled up. Missing ones allowed the head studs to turn out with the head nuts.
o Push Rod tubes installed with the seams facing down, ancient seals shored up with globs of RTV silicon.
o Rings on cylinders set up with gaps aligned, some oil rings with gaps aligned and facing down.
o Cylinder base gaskets bent mangled, and leaking severely.
o Silicone rubber cement (RTV) everywhere, used during assembly and also, it appears, after as an attempt to shore up some of
the leaks.
I could go on, but you get the idea. Turns out #3 was just poor assembly, lapping cylinders to heads and properly installing
gaskets. Now a solid 145 lbs of compression there. A pleasant discovery was a big bore kit in fairly good condition. We
left the rings in place (the ones I bought were standard ones anyway) and reassembled. Good finds were a solid blower fan,
newer gland nut with needle bearings, a leak and crack free oil cooler, and a generally leak free case. A 12-dollar 200mm
clutch disk installed to replace my slipping glazed unit solved the slip issue with pressure plate and flywheel resurfaced
with a sander to remove some of the glaze. The engine still needs to be tuned, but I am hopeful this will buy me a few
thousand miles.
11/05/03: Well, the new Speedo is in and works great. Glass is clear and accuracy is good. For the first time I now have a
working trip odometer. The plastic horn grills look good, I am happy. The old ones were very tired and this spruces up the
front enough to make due. Now, since the last installment, my clutch has started acting up some, slipping. No amount of
adjustment seems to help, I simply need a new clutch disk. I have ordered a 200mm VW disk that is supposed to be the same
with a little less wear surface. We'll see. I also plan to pull the heads over Thanksgiving week and do a limited top end
rebuild/repair. The 22nd I will pull the motor, separate the tranny, and yank the heads. Until then, it's all guessing!
10/2/03: New Speedo is waiting at the house, need to clean glass and install. Last weekend I was able to get the drivers
door aligned pretty well so it no longer gaps at the rear. I also have a set of used plastic horn grills in the mail that
should be an improvement over mine.
9/22/03: Over the weekend I worked on getting the clutch readjusted again. Since reinstalling the motor, the engagement
point of the clutch has been uncomfortably high and has caused me some concern over the possibility it may not be fully
engaging at the top. It hasn't seemed to have had any issues so I think that there was no damage done. I have had the
linkages apart a number of times and now was running out of adjustment under the car at the clutch fork, meaning I needed to
go into the tunnel to adjust the link at the pedal end. In the tunnel, you extend the cable length to engage the clutch
sooner (closer to the floor) just like at the tranny. I had plenty of adjustment room there and with a little tweaking on
the cable and the clutch stop at the floorboard, the clutch now engages nice and low while still not grinding when the car is
shifted into gear.
Another issue has reared its ugly head, as these things will often do. My Speedo has been intermittent and now seems to have
stopped working all together. I had it out and apart yesterday and the only thing I can come up with is that the drive where
the cable feeds in appears to be pretty worn at the outside end. This leads me to believe that the cable itself may not be
reaching up inside the unit far enough to engage the drive and operate the instrument. Short term, I tried sleeving the
cable end in foil to slightly enlarge it in the hopes that this would engage the Speedo drive and allow the unit to work. I
did not have a chance to try this yet, but I am not very hopeful and think that the solution is going to be eventually
getting a 'good' used unit to replace mine.
9/7/03: I have moved my Journal over to the Lone Star website today. It was just getting to be too much trying to maintain
two sites on the same topic. I will gradually tear down the other site and move the data here. Today I replaced the battery
under warranty as it was leaking acid allover my car. AARGH! After a scrub down with baking soda and water to neutralize
the effect of the acid, the new battery was installed. I also re-wired the hot start relay again. After visiting with Sid
Leben yesterday for a while, I bought in on his take on the purpose of the relay. I now use it to allow me to pick the
starter solenoid relay with battery voltage by picking the additional relay with the switch or yellow engine compartment
wire. The hot lead is back on the starter instead of off on the secondary relay and the car seems to crank faster..... I
also pulled off one of my torsion bar covers. Mine seems to have the rubber bushings that are not vulcanized to the metal.
I pulled off the drivers side only and rotated the worn bushings for now so that the thicker portion of the rubber is up
instead of down. I decided I will buy new bushings when I have a little extra cash and do the job right, lowering the car at
the same time. Not today, however. I also adjusted the clutch cable. After the drive yesterday, I realized I was engaging
too high and now have it back down near the floor where I like it.
9/5/03: With the car back together now, I needed to do a bit of tuning before it would be ready for 130 miles of driving
tomorrow for our trip to Giddings. With the new carb top from Parts Obsolete installed, I set my float levels for the first
time. For some reason this has always seemed like a daunting task, and I have put it off for way too long. It only took a
little playing around with the adjustment screws with the float bowl plugs out to realize two things. First, it was brutally
apparent that I was running the car with the float bowls WAY low. The second was that there was no way I was going to get
the floats set high enough with the current spacers on the fuel check valves. Off came the carb tops and the spacers on the
check valves get replaced with thinner ones. These allow me to get the right carb dialed in and the left one set about right
with the screw at the max height adjustment. I put some loctite on the threads of the adjust screws for insurance. Now the
car will idle pretty smoothly down to about 900 RPMs, and the transition from idle to the mains is smooth. Cool.
August 03: Since I have been negligent in my updates this will be a bit brief. The engine was removed and a superficial
examination of its condition was made, which revealed nothing significant. The engine was degreased, leaking drive shaft
seal replaced on the tranny, and both CV axles were disassembled, cleaned, repacked and new boots applied. The inner joint
on the passengers side is the only one that seemed particularly weak, with the normal interference fit of the ball bearings
weak and in some cases gone. I drive the car only a little still and there is no clicking from the joint so I elected to
clean and reassemble as is for now. While the motor was out, I also installed one of the new metal cased throttle links in
place of my rubber one. The rubber piece was still in good condition so into the toolbox it goes as an emergency spare.
Soundproofing was added to the engine compartment while the motor was out also. This is MUCH easier than working around the
motor and the results are impressive. Its now possible to carry on a conversation while driving without screaming at the top
of your lungs!
July 03: The driver’s side rocker panels were removed and replaced. The dash was repainted, gauges cleaned, and a new dash
pad installed. A new windshield and seal were also added, with the windshield wiper motor being removed, cleaned, and
reversed to park on the original drivers side. I also repainted the wiper arms in silver. The washer pump has been
renewed, new washer nozzles and lines added to make the system work again. Though it pumps fluid now, most of it ends up
rocketing over the car to nail anyone standing nearby. I'll need to work on this but for now at least I have an operational
system.
6/11/03: Lots of progress, very little of which can be seen from the outside. New shocks in the rear, new struts up front.
I replaced the old door plugs with fresh ones and added the rubber boot to the passenger’s side some light switch. A second
ignition key has been cut and a buzzer added as a headlight on reminder. A brief compression test reveals that the #3
cylinder is still hovering around 100 for compression. The front end has been aligned successfully. Current plan is to get
the rockers replaced and start prepping for paint. I plan to do a DIY paint job in the garage by fall... we'll see how that
goes.
4/13/03: The fuel tank is back in, the bumper on, and the car is running again. The car now has much more of a solid feel
to the steering but it is in dire need of an alignment.
4/12/03: Kevin Weldon came down from Dallas and helped me weld in some structural support to the front suspension pan. I
also replaced some of the dash wiring to clean up the POs hacked in repairs.
4/9/03: The seats are repaired, mechanisms tightened, and installed in the car. They look good.
4/6/03: Soundproofing installed in the floor in anticipation of installing the new seats. This should make the car quieter
overall. The material is covering the entire floor and tunnel. I also attached a piece to the inside of the shift coupler
cover.
4/5/03: The bottom of one of the new seats has some seam and material failure that I repaired from the inside by removing
the cover and sewing it up. There are also some small tears in the sides of the seat bottom that I will repair with a
Permatex vinyl repair kit. Much better than leaving holes.
4/4/03: My "new" seats are here. This is a trade from a fellow in New York who wanted original seats and had a set of early
70s buckets in good condition. We traded for the cost of shipping, a mutual good deal.
2/25/03: replaced the square tranny mounts with a good used pair. Mine were cracked about 30% through and these look good.
2/23/03: Tuning, Tuning, Tuning. I got my 050 disty so it produces about 30-35 degrees of advance at around 3300 RPMs.
This helped my power output considerably. My idle is now up to around 1200 RPMs, so I need to back that off and resync the
carbs. I also removed the slack from the throttle linkage. Previously, you needed to depress the gas pedal about an inch
before it affected the carburetor linkage. Now it's closer to 1/4 of an inch, and the car feels much more responsive. The
clutch is now adjusted to my liking also, with a low engagement point and still no grind between gears. I have a worrisome
whine in my tranny when the clutch is down that's probably throw out bearing going out.. hopefully that Swepco 201 helps it
hang in there. We also stuffed the seats to raise the driver elevation by using a small square pillow in the middle and
stuffing batting material around it. The increased height definitely makes for a more pleasurable driving experience. It's
starting to feel more and more like a real car.....
2/9/03: I lowered the front end to where I think it should be. Looks much better but I need to bring the rear down also.
This is more complex and I want to replace some bushings and repack the wheel bearings while I am in there. I also adjusted
the clutch. In this process, I discovered another weak point on the car's design I was not aware of. The clutch cable is
attached to the clutch fork by a plastic part that can break and leave you disabled. I pulled the worn part from my car and
made a steel one from a 60-cent part I got at the local hardware store. I saved the old plastic part as it would still work
and would get me going in an emergency.
Finally, I discovered that my inner generator pulley wheel is failing again.
This is the third one for me and I can see now that the issue is a worn hub. I will attempt to get the old hub off and renew
it along with what I hope will be my last inner pulley half for a while.
1/31/03: Seals on front wheel bearings,
reinstall. Lower front end (1.5 turns each bolt), bleed brakes.
1/25/03: Pulled front hubs apart to pack front wheel
bearings. Bearings appear to be in very good condition so I just ordered seals. Should have them by next weekend. Also
working to address a seeping connection on the brake master cylinder.
1/21/03: installed correct blower to heat exchanger hose, replacing the blue RV drain hose I have been using for the past
year.
1/19/03: Pertronix Electronic Ignition installed, along with a 40KV flamethrower coil. The car now starts much better and
idles down quickly. Thanks Santa!
1/17/03: The Window is back in and works well. Ready for tomorrow's rendezvous! I also have a new rubber strip on the
outside of the passenger’s side window.
1/7/03: Drivers side window regulator failure. 70 bucks in parts from Tweeks on the way. Glass okay, regulator failed.
Ordered new felt for channel and other parts to renew mechanism. Hopefully will get before the weekend.
1/5/03: New 050 Distributor, 009 is out. Dash has been covered in felt to hide the uglies and I am recalibrating the clock.
That should go back in next weekend.
12/13/02: I installed a new muffler to replace the hacked in Dual Exhaust. It is now much quieter and looks more stock.
Also looked at the general performance of the engine decided to address some of the spark issues as a possible source of my
performance issues. A new 050 distributor, coil and electronic ignition are in my near future.... or at least once I get the
exhaust work paid off. They did ok at the shop but the bill says they saw me coming....
11/29/02: I added a radio to the car. The dash had already been hacked past original dimensions so I used a cutting wheel
on a dremel tool to make a DIN size opening and slid a discount CD player in the opening. A couple of 4-inch 70W pioneer 2
way speakers are mounted just above the storage pouches in the front foot area. No noticeable engine interference and sounds
acceptable.
11/20/02: FINALLY got an air compressor for the garage. A 6HP 21 Gallon with an upright tank. Have an impact wrench, air
chisel, tire inflator, and blower nozzle so far.
11/15/02: 2 new tires to replace the old dry rotted ones on the car. 195 65 15 s seem to be a nice fit. The car will sit a
little lower than the Metrics that were on there would allow and these are slightly wider too. Need a couple for the rears
but $$ will pace that....
8/18/02: Well, the tank is sealed, painted, back in the car and full of fuel. No leaks so far so hopefully we're done with
that for a while. I have driven the car some and the only performance issue appears to be a fuel starvation issue after a
period of hard acceleration which leads me to believe that either there is an improperly adjusted float or floats in the
carbs from my rebuild or that the mechanical fuel pump can't keep up. I leaned out two cylinders slightly which showed some
of the telltale black greasy residue on the plugs indicating they were running rather rich. I also did a compression check
which yielded a cylinder on each bank with low compression. My noisy valves leads me to hope that its still gunk and not
rings- 2 of the 4 are in the 145-150 range and the other two are around 100-120. So, I changed out the oil, which came out
like tar after only an hour or two since the last change and added some Marvel Mystery oil to the crankcase and a fresh fuel
and oil filter. Will pick up some MMO today and add the prescribed 4 oz to the gas today. Next is to drive it a little and
see if it cleans itself up. I'll attempt to get 100 miles or so on it, change the oil again, and then see if the compression
rises. If not, I need to make plans to pull the engine and start on the overhaul.
8/4/02: Well, yes, I still have the car. Haven't been working on it since mid April due to some other things taking
precedence, but have gotten back into it a little over the past few weeks. A nagging pinhole leak in the fuel tank has been
fixed by a local radiator shop and we are now in the process of stripping the rubberized coating from the tank so it can be
properly rust proofed and painted. The coating is difficult to remove, using chemical strippers and elbow grease. Once
complete, it will go back to the radiator shop for a thorough cleaning and a final check for leaks. After that, its
rust proofing, prime, and paint, then back in the car.
The pedal cluster has also been rebuilt and reinstalled in the car. New pedal rubber and bronze bushings should make for a
vast improvement in functionality. A broken and welded / repaired clutch actuation lever worries me - it seems solid but
mark my words, this will probably be the first thing to strand me by the side of the road. :-)
2/24/02: Well, this weekend, I adjusted the valves. The process is pretty straightforward and I was able to figure out
everything without any difficulty. The first cylinder to adjust, #1, is the one that wouldn't fire. I started with the
exhaust valve, set the gap, and rechecked the gap. Next, I went to the intake valve. The valve was sitting back slightly.
When I moved the gap adjustment set screw, there was a "ping" and the valve seated. Now, the car seems to run on all 4
cylinders. I have yet to do a compression check and the carburetors still need alot of work, but things are looking more
promising.
The Fuel tank is still holding, no troubles with leaks. The fuel gauge-sending unit is a little intermittent, I'm hoping
it's just sticky and will loosen up with use.
Today I reinstalled the safety belts and front trunk carpeting. The safety belts are really clunky. They do have shoulder
belts and lap belts, but no retracts and adjustment is difficult and manual. Still, it will keep me legal for now and safer
than without.
Coming up next is the carburetors. I have kits for them and need to find the ambition to dig in. I am sure they have
plugged jets, bad seals, etc.... At a minimum, I will put in the new parts I can without major disassembly and try to clean
the jets.
Its fun to be able to drive the car finally. Now, each change I make can be measured against previous performance, or lack
of it. I'll let you know.
2/21/02: I've been failing pretty badly here at keeping up with my list of activities over the last month. Here's a list of
what's gotten done since the 6th of January:
We patched the hole in the floor of the front trunk with new steel but after looking at another local 912 here in Austin, I
see that there may be issues with a structural brace that was also damaged by leaking fuel. A repair panel is available, at
a price of course, and should be installed before any significant driving is done.
New fuel tank is in the car and working. I had the inside sandblasted clean and have scraped the loose rust from the outside
and treated it chemically. I repaired a pinhole on a seam with some JB Weld and sprayed the whole thing with truck bed
liner, along with the under hood area, which also had its fair share of surface rust. The fuel sender in this tank works and
I now have a functioning gas gauge.
I was able to get the new fan belt on the car. Adding or removing shims from between the generator regulates tension
pulley wheel halves. After a bit of operation, I see the belt tension needs to be increased so I will need to adjust that
before too long.
Floorboards have now both been scraped down, treated for rust, and the seats are back in on both sides. Floorboards are not
structural on a 912 and these seen solid, so I am done with this for a while. I also got a coat of black oil paint on the
wooden floorboards so they are done now too. These boards sit at an angle up by the firewall and hide the pedal cluster and
some of the wiring.
The engine is next. I have it running on 3 of 4 cylinders. The 4th one worries me. I have spark and fuel but the cylinder
does not fire. This leaves compression, or lack thereof. This weekend, I will check the valves in the hopes that there is
something dramatically out of adjustment or maybe a broken valve spring. After the valves are adjusted I'll do a compression
test and we'll see. It might be time to start thinking about an overhaul......
1/6/02: I decided to try to get the thing to run a little better. I set the breaker point gap, and adjusted the timing as
per original specs. I think it is interesting to note that the manual recommends setting the timing with the engine off.
This is accomplished by aligning the timing mark on the block and the flywheel and backing off by 9/64 of an inch or 3
degrees, marked by me with a steel rule and a pencil. The distributor is then loosened, the cap removed and a 12V test light
placed between the contacts. The distributor is then set to the exact point of contact and tightened down. I also put new
plugs and plug wires on the car. The old ones didn't look that bad, but with no maintenance records, it’s hard to say when (
or if) they've ever been changed. With that done, I bolted the rear tires on it and after a small battle with the sick old
carburetors, was able to get it to start. We took our first drive, just to the end of the block and back in first and
briefly second gear. Performance is still awful but it was still great to drive it again, it gave me hope for things to
come!
1/5/02: The brakes are done. My rear brake lines turned out to be the wrong part. The inside fittings needed to be male
threads and the ones I was shipped were female. Today I now have the correct lines. They installed with little to no
difficulty, especially when compared to the removal of the originals. With a little help from Cindy, I was able to bleed the
brake system and get sufficient pedal firmness and solid grip/release action on all four corners. I then was able to bolt
the front tires back on the car and drop the front back on the ground for the first time since October.
1/1/02: I sent the check off to a spare parts reseller for a used fuel tank to replace my old one. For now, it’s running off
of 2 gallons of fuel in my lawn mower can strapped to the sidewall under the hood. My neighbor has a welder and a plasma
cutter and has volunteered to help me with the rust hole in the front where the leaking fuel ate through the floor of the
trunk over time. This will be done before the tank is installed so there is no risk of fire. After that, I'll clean up all
the surface rust under the hood and apply a coat of rust inhibitor and black paint to preserve the remaining metal.
12/30/01: The floorboards that sit at an angle in front of your feet are made of plywood. Over the years, moisture has
gotten to these and the glue between the layers of wood has come loose, leaving them weak, separated, and flimsy. The
driver's side boards are rather difficult to reproduce as the wood is bent in a curve as it goes up towards the dash. By
gluing and clamping these over the last two weeks, I've gotten these back in pretty good shape. When the weather warms a
little, I'll sand them and soak several coats of oil paint into them and they should be serviceable again.
12/29/01: I decided from the amount of particulate matter deposited behind each of the pistons in the rear calipers that I
needed to get the rear lines off one way or another. To get the old ones loose, I resorted to some relatively drastic
measures. I took a tin snip and cut the rubber lines off where each met up with its inboard fitting. I then was able to
slide a deep well socket over the end of the metal fitting and break them loose. The passenger side, where it feeds into the
tee box, was relatively easy. The Tee is securely mounted to the body of the car so I was able to apply a great deal of
force without worrying about damaging the car. The driver’s side is a little different. The steel line can turn behind the
flexible line so I needed to enlist the help of my friend Russ Minnick. I laid under the car and held the steel line still
with a box end wrench while Russ put the socket over the cut off line. With both of us using about all the strength we had,
the line finally came loose.
12/16/01: Right rear brake is done and I have a good start on the left one. Its looking like the rear brake lines are going
to be a nightmare. I can't get the drivers side one loose at all and getting a wrench on the passenger side is not possible
where it’s at right now. I'm told I can loosen a bracket on the passenger side and the driver’s side may require a vise grip
and some heat from my torch. We'll see. I may be forced to wait until the engine comes out so I can access it from the top
and take my chances with the old lines....I'd rather not do that.
12/7/01: Front brakes are done. The car's up on jack stands all the way around now, with the tires leaning against the
garage wall. I applied a dose of WD40 to the fittings/bleeder valves and mounting bolts on the back to soak overnight.
Status of the front: Apply brakes, wheel stops spinning, release brakes, wheel spins. What more do you want!
11/29/01: I got the outboard piston back in the caliper and the inside one loose and ready to clean it up. Maybe there is
hope. Also cleaning up corroded chrome here and there along the way. Discovered that the engine is running on less than
the required 4 cylinders. No time to look further at this point but could be plugged carburetor jets, bad plugs/wires, or
something simple like that. For now, that's what I am hoping anyway.
11/18/01: I'm up to my elbows in the driver’s side front brake. Caliper off... replaced flexible brake line with new
stainless steel line. I've got one of the pistons out of the caliper and am now discovering the same problem many other
folks have had with the "spring" in the piston. I need to hit the 912 Registry and get some help. Brake pads look really
good so I can save some dough there, assuming they are good on the other side too.
11/16/01: Installed a new Brake Master Cylinder. Added fluid to the reservoir and the system holds pressure. Cool. Next
step is to dig into the first caliper.
11/3/01: Stripped out the insulation from the floorboards and went after them with a wire brush. After a thorough cleaning
of the driver’s side, where most of the rust was, I gave it a liberal dose of rusty metal primer and black paint. Now need to
get replacement insulation for the floors. Also cleaned and repaired the upholstery on the drivers seat while it was out.
Doesn't look too bad.
10/27/01: A friend and former mechanic comes over to help look at the brakes. We put a little fluid in the reservoir and
out it comes from the lead in hose to the master cylinder. Decided seeing as a brand new Master Cylinder can be had for
under a hundred bucks, this one should be written off. We remove it with little difficulty and set it aside.
Next project was to get some fresh fuel in the gas tank. As we began to pour in fuel, we note a dripping sound..... turns
out the tank has a major rust out at the top of the spare tire hump. A huge mess follows and the day ends with about 7
gallons of stale fuel in buckets and the tank pulled out of the car, As a side note we see that the fuel sender is shot too.
All part of the game.
10/21/01: Sunday morning, out back doing some painting on the house. Phone rings. Truck transport driver calling from
about an hour out with the Porsche onboard. Reality time. Today we find out what I really have.... and don't have. Pretty
soon the guy arrives, have to give him directions several times via cell phone but he gets there. The pictures on the
Porsche Pictures page show the story.
10/18/01: The transport picks up the car late in the day. John comments that he has to load the car himself which is a
challenge because the car has no brakes. This is the first I've heard of the no brakes comment so I am a little concerned.
Hit the internet and price out brake parts...... all are pretty cheap so I figure that rebuilding brakes will be the first
task.
10/17/01: On the phone most of the morning. Making arrangements with Lone Star Auto Transport. Yes, they will have an auto
transport in the Bay area this week. Yes they can deliver the car to my doorstep. Yes, they take only cash or money order.
Yes, this is getting expensive. Also, Fedex on line tracking confirms that my check has been signed for in California. They
now have bunches of my dough, and all I have is a few pictures and some promises.
10/16/01: Off goes the Cashiers Check to John in sunny California. The shipper also calls and says he wants to pick up
tomorrow instead of Thursday. I quickly conference in John and arranged the pickup. Should be here by early next week.
10/15/01: Frantic exchanges of cash take place, all of it flowing away from me to people I have and will never meet. Shawn
in Arkansas gets his broker fee wired to him and he puts me in touch with his partner in the San Francisco Bay area. I get
the last of my questions answered about the car and agree to send a cashiers check (don't Ask$) FedEx to him. I also get in
touch with a shipper out of Dallas who can pick the car up on Thursday or Friday of the same week. Money moves from a Money
Market account at a financial firm to our bank so I can get a cashier's check in the morning. Shawn also closes down the
auction on E-Bay. He has me bid the reserve and closes bidding. That way I now have a feedback rating of "1" instead of "0
". This will help assure other sellers as I go hunting for parts in the future.
10/14/01: I send this seller a couple questions about the 1967 912 he's got listed on E-Bay. It looks pretty straight and
original. I figure I'll check it out and maybe place a bid. I lost a '66 in the last 10 minutes of an auction a couple
weeks back so I'm a little gun shy of the whole thing. About an hour later I get a reply. He'll sell directly to me and end
the auction if I give him below his reserve price. Cindy and I talked about it in great detail. She must be even more nutz
than me because she agrees to let me go for it. I send him a reply agreeing to his terms and an hour later we're working out
details on the phone.
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